Archive for the ‘projects’ Category

TPS replacement

9 November, 2009 06:00

No, not the TPS report from Office Space but the throttle position sensor in my daughter’s 1993 Olds Ciera.
The Check Engine light was on last time she was here. We read it out with the Actron CP9135 scan tool . The code 22 indicated that the voltage on the TPS was low. Since this is a 1993 Oldsmobile Ciera, replacement was probably indicated.
She brought the part with her for this visit.
The TPS on this 3.3 MFI engine faces down toward the upper radiator hose pipe. No clearance for a normal screw driver. If we had had a flat ratchet offset style driver, that would have been ideal. Lacking that, after disconnecting the battery and removing the air cleaner and its mounting plate, we used a needle-nose vise grip to break the 2 screws loose. Then used a #1 Phillips tip in a holder to get them out. Replacement was a matter of holding the screws in the TPS while aligning the paddle that is pushed by a similar paddle on the throttle shaft. Starting both screws by finger, running them in with the mini screwdriver and snugging them with the vise grip. Reconnect the battery and test. Put the air cleaner mounting plate and air cleaner back on. Clamp the air inlet hose where the strap had broken and done.

Flower Flyer Rebuild

17 May, 2009 13:46

The Flower Flyer started as a re-build.  My wife had found a rusted coaster wagon in someone’s trash and dragged it home.  I built a body for it and painted it green.  Phillip made a stencil and painted Flower Flyer on the sides.  It was a pretty thing.

But the outdoor storage was hard on it and it developed dry rot.  Time for a new body.  I was sure that I had a picture of it but cannot find it.  After I took it apart, I took a picture of the body as it was.

Flower Flyer body

Flower Flyer body

Using a sheet of 3/4 inch plywood and higher 1×6 pine sides, I built the new body.  This time I put scuppers in it so the body would drain better.  I used brass screws to reduce the rust and the start of rot.  I also treated all of the parts with linseed oil and pine tar before assembly.  Here is the new Flower Flyer.

Rebuilt Flower Flyer
Rebuilt Flower Flyer
Scupper Detail on each corner
Scupper Detail on each corner

Austin Healey

4 January, 2009 14:50

I took some pictures of this great restoration of an Austin Healey 100 yesterday. John Burton is a neighbor has spent years working on this. The results are definitely worth the effort. What a great job. Additional pictures in a new window. My son took some of the pictures while the hood was open.
Austin Healey 100

Making Glass Beads

2 January, 2009 17:57

Jeannette making glass beads on a torch flame

My daughter was home for the holidays. Most of the days were rainy but we had at least one nice day when we could be outside. She took the opportunity to make glass beads. My son took this picture. The glass rod is melted and gathered on a mandrel, additional colors are added. The bead is then cooled slowly.

License Plate Light

21 December, 2008 11:47

A neighbor stopped me to tell me that my license plate light was out.  I thanked him and said that I would take care of it.  That was almost two weeks ago.  Last weekend, I did get the correct bulb at the parts store but did not get it changed. Here is what I did yesterday.

The socket itself is retained by two small TORX screws.  I have two drivers but it was smaller than either.  I got a bit from the “security bit set” that I had recently purchased at Harbor Freight.  This kit contains an assortment of sizes of every odd bit for odd screws. The kit has a 1/4-in drive bit holder.  I used a 3/8-in drive extension and a 3/8-1/4-in adapter to make a screwdriver to remove the screws. The lamp housing was stuck to the license plate recess so I used a putty knife to gently separate it.  The lamp was cracked but came out easily.  It was clearly burned out.  The housing was also cracked, problably from frozen water.  I sealed it with Goop brand sealant/glue. When I inserted the new bulb, it did not make contact initially.  There was some grease or silicone gunk that kept it from making good contact.  Wiggling the bulb got it to work.  Re-assembly reverse of disassembly.  Phillip and I also checked all of the lights on all three cars and topped up the mini-spares.

Icemaker Repair II – part 2

3 May, 2008 09:29

The previous post talks about the problem with the ice maker. This is about the fix.
Basic ice maker theory. 1. Put water in a container. 2. Put it in a cold place and 3. wait until it freezes. 4. Warm the container until the ice is loose enough to come out. Repeat.
Automatic ice maker theory. Actually begins with step 3 since this is where you will find the automatic ice maker most of the time. There is a thermal switch that detects when the container (and the ice inside) is at a frozen temperature. When this happens, the switch closes and the motor rotates the paddles. A switch turns a heater to warm the ice mold to loosen the ice. The paddles push against the ice.. The motor will push the paddles against the ice until the ice releases. When the ice releases, the paddles continue around and push the ice into the catcher. At some point the heater turns off and the water is turned on to refill the mold. There is a small slotted adjuster on the side of the unit that sets the amount of water and hence the size of the ice chunks.
My unit was somehow jammed. I poured about 1/8 cup (.03 liter) of water to get the cubes loose. The paddles rotated and the cubes came out. It refilled normally. The water going in made a noise like the mold might have been really hot. The ice made in about 20 minutes and came out normally. I reduced the cube size slightly (clockwise 1/16 turn of the slot with my thumbnail) to reduce the force required to push out the cubes.
It is still working a week later.

Chairs

27 April, 2008 20:55

Our dining room set was moderately expensive 25 years ago. It has held up well. But it is “factory made”, not “craftsman made”. The worst part of the factory is the machines that shoot staples and some sort of flat metal thing into the joints. These make repairs impossible. These items probably stabilize the joints while the glue dries. Because they are impossible to extract and damage the wood when they go in, they weaken the joint to begin with and make repairs impossible later when the joint lets go. I would recommend that Congress ban the domestic manufacture of furniture using these devices and the import of same.

Chair Repair

18:38

Today’s project was the re-assembly of a chair that was disassembled 3 weeks ago. The nature of chair assembly is that once you begin, you must finish all of the stick together parts in one session. The screw together parts can be done later but because of the way chairs are, they need to go together all at once. Allow adequate time. The three week lag was because I did not have a clear spot on a weekend long enough to keep it open ended.Let inertia work for you.

The first step in chair repair is get the chair completely apart. If the chair has failed catastrophically, there may be broken parts along with parts that are still quite tight together. If the chair is just wiggly and loose, many of the joints are probably ready to come apart with the appropriate amount of force. It may be difficult but you must make sure that you have all of the pieces that will or can come loose, loose.

IMPORTANT – as you remove each piece, mark it so that it can be re-assembled in the correct orientation. Make the left of the chair as you sit in it the left. Mark each piece in an inconspicuous spot with Front/Left/Top etc. so that you cannot be confused when it is time to assemble.

CAUTION – watch for modern short cuts that may render your chair difficult or impossible to repair. Staples, pins, repair plates, steel wedges are difficult to remove, damage the wood fibers and are the topic of another future blog entry.

Disassembly proceeds easily at first and then becomes more difficult as the pieces get harder to separate. For large pieces, this can mean working them apart by pulling and wiggling. I find wiggling the piece in a rotating pattern with occasional reversal of direct the most effective. Sometimes rocking side to side is best. Rarely, you may need to wedge some like a stick of wood where the scars will not show and leverage against it to get movement.

Another technique is the tap. Tapping with a rubber mallet can do the trick. Mine is white rubber and does not mark. A hammer, carpenter’s hammer or machinist’s, provide a firmer force. Protect the struck piece with a smooth piece of scrap. The sharp blow of a hard hammer may be more effective at breaking a glue joint. Let inertia work for you. Watch the rebound.

Once you have all of the big pieces apart, try and get the pegs out. Grasp the peg with a pair of slip-joint pliers. See if there is any movement at all. If there is, try to work the peg out its hole. If there is no play and tapping does not loosen it, skip it.

Inspect the pegs. Replace any that are cracked and those that have left a chunk in the hole.

Check the holes. Clean them out with a drill of the appropriate size. Remove any glue left in the hole. Modern glues may not stick to themselves or other glues. Old glue, such as hide glue needs to be renewed so get it out of there.

Clean up the ends of the rungs and the holes in the spindles and rails. Use 60 grit or 40 grit sandpaper to get the glue of and the pegs and pieces smooth. Get everything cleaned up for smooth re-assembly.

Once you have it apart, lay out the parts in the order that you are going to assemble them. Some chairs have to be assembled all 4 corners at once. Others like the one I was working on today can be assembled from front to back or back to front.

The first assembly is a dry assembly. It helps you to do the final assembly correctly and easily.

For my chair, I joined the two front legs with a rung, 4 pegs, and the front piece. Observe the surfaces and the left to right orientation. This I laid flat on the floor. I then added 2 rungs and a side piece on each side.

Separately, I assembled the back. There were 4 back slats, the back seat support, and a rung (which I could not get out). I then put the back onto the front. I noticed as I was doing this a hole that retained a piece of the peg. An I had replaced the peg with a fresh one because it was split. If I had been working with glue, I would not have had time to clean up the hole and get it together before the rest of the chair got too stiff to work with. This is why we do a dry assembly.

Work out how you will put the clamps on to pull everything up tight. You may want bar clamps ( quick-clamps work well) or a rope clamp. I used both.

Take it all apart again and lay it out neatly.

For the final assembly, I used Chair-Loc . I have used this in the past and it is good for about 7 years of daily use on these chairs. The chair I worked on today did not get completely disassembled last time I did repairs and so it has never really been tightened up in 25 years.

Repeat the assembly this time putting Chair-loc in each hole and spreading it around each peg or rung. Press everything together. Clamp it, tap it and get it real snug.

Give it a while to set up, put the seat on and screw in the screws.

The chair is now nice and tight.

Cat Bed

22 March, 2008 19:05

I have made a number of beds for the cats. This is a fairly quick and simple project. You need a table saw or a router with a 1/4 inch cutter that will cut to 3/8 inch depth.

I noticed that the cats liked cardboard and corrugated boxes and box lids of a certain size. This is the size that I made the box out of wood. The sides are a little higher than the preferred lids but my wife makes Polar Fleece “puffs” to fill the bottom and the cats seem to like them.

The first box lid that the cats liked was the tray that came in the citrus fruit from Florida. This tray had doubled sides and seemed to be a particular favorite of the cats and so became the model for size and proportion. This one is 16 by 10 1/2 inside. This makes the length 17 1/2 and the width 12 inches.

The basic idea is simple. Four sides and a bottom. The bottom is fairly fixed. It is 1/4 inch plywood. The sides give lots of options.

The first option is the choice of material. Pine, oak, and cedar are good choices. Pine is inexpensive and easy to find and work with. Oak is pricey and pretty. Oak looks good indoors and ages gracefully outdoors. Cedar is rot resistant and can be pretty. Not too expensive but cedar splits easily if the corner screws are over tightened. The height can by the 5 1/2 inch width of 1 by 6 or the 7 1/2 inch width of 1 by 8. And a couple that we have are from 1 by 4. Of course the 1 by is 3/4 inch thick.

The box construction is straight-forward. A rectangle with the long sides (length) overlapping the ends (width). The bottom is set in a groove around the bottom. The groove is 3/8 inch deep in the 3/4 inch thick sides. Cut the plywood about 5/8 inch wider than the width and 7/8 inch shorter than the length.

For the box above, this would be 2 pieces 17 1/2 inches and 2 pieces 10 1/2 inches. The bottom is 16 5/8 by 11 1/8.

NOTE: Follow all general and specific safety instructions for the tools you use.

Cut the side and ends to length. Set the saw blade (or router cutter) height to 3/8 inch above the table and remove the splitter so that you can dado a grove. Be very careful if this leaves the blade unguarded. Check the height with a piece of scrap and adjust it until it is just the right height. If you are using a router, you and your router may be happier and your cutter may last longer if you make several passes increasing the depth until the final depth is reached.

Set the fence so the close edge of the blade is 3/8 from the fence. Carefully make a pass through each piece. If you are using a 1/8 inch saw blade go on to the next step. If you are using a 1/4 inch router cutter, skip the next step.

Reset the fence so that the far edge of the blade is 5/8 from the fence and just a scosch more. Test it with the scrap. Try the plywood bottom for fit in the slot. If it is loose, move the fence closer. If tight, move the fence a bit farther way. When adjusted, make sure that you hold the previously cut edge toward the fence and carefully make a pass through each piece. When you have cut both sides, you may need to clean out the bottom of the groove with a 1/4 inch chisel.
You now have a 1/4 inch groove in all 4 pieces.

Trial fit the sides and ends against the plywood. The plywood should fully close the bottom. The sides should mate up tightly against ends.

Drill and countersink a hole in each side 1 1/4 inch from the bottom and another 1 inch from the top. IMPORTANT: Assemble with brass screws. Steel screws and galvanized screws will leave stains on the wood. Brass screws will turn a pretty verdigris if they do anything.

Line with a blanket made from Polar Fleece. Make sure that there are several thicknesses and that the ends and sides of the liner extend beyond the wooden sides.

Reviving the Hammond

01:11

I have a Hammond organ. I have had it since my dad moved it from his garage to my house in Connecticut. Before that it had been in my grandparents house. I used to play it occasionally in Connecticut as did my wife. But since we have lived here, it has been played maybe once. My wife re-arranged the room that it is in about 8 years ago and the speaker cable got disconnected and it has not been powered on in all that time.

Tonight, my son, 17, decided that it needed to be played. We had tried it a couple of weeks ago and knew that it was stuck. The oil had dried out and it was not turning when the start switch was on. Tonight when his friend was here, they picked it up and moved it out a bit from the wall. I took the back off and loosened up the rotor shaft. The start switch would get it to turn but it would not run. I got some light oil and put it in the oil cups. It dripped down the tubes and into the wicks. Still no go. We went and did something else for about half-an-hour. Now it ran but the bearing was still a bit noisy. After a minute of playing, it settled down and was quiet. Phillip played it for about an hour trying various combinations of drawbar settings. Quite exciting. This little bit of machinery and electronics was made sometime between 1935 and 1940. The predecessor of the Hammond B-3. We need to make sure that we play it often and that we oil it with the proper Hammond Oil next time.